Description: Front saddle stapler home position error: The stapler home position detection is abnormally operated and finished. [MJ-1108]
Causes: Front saddle stapler clinch unit Saddle control PC board
Remedy: MJ-1108 Front saddle stapler clinch unit Harness check Saddle control PC board (SDL) • Connector check (CN4) • Board check
Code: CBB0
Description: Rear saddle stapler home position error: The stapler home position detection is abnormally operated and finished. [MJ-1108]
Causes: Rear saddle stapler clinch unit Saddle control PC board
Remedy: MJ-1108 Rear saddle stapler clinch unit Harness check Saddle control PC board (SDL) • Connector check (CN7) • Board check
Code: CBE0
Description: Saddle Stitch Finisher folding motor (M17) abnormality: The folding motor is not rotating or the folding roller is not moving normally. [MJ-1108]
Causes: Folding motor encoder sensor (S34) Side alignment motor (M15) Saddle control PC board (SDL
Remedy: MJ-1108 * You receive a [CBE0] error when the [EF17] error occurs three times in succession. Folding motor encoder sensor (S34) • Sensor check (S34) • Connector check • Harness check Side alignment motor (M15) Harness check Saddle control PC board (SDL) • Connector check (CN11, CN14) • Board check
Code: CC02
Description: Stack exit roller nip home position detection error [MJ-1036]
Causes: Stack exit roller shift motor (M6) Stack exit roller home position sensor (S13)
Remedy: MJ-1036 The stack exit roller home position sensor (S13) does not detect that the exit roller is not at the upper position after the stack exit roller motor (M6) has been driven in the specified time when the exit roller is moved down. The stack exit roller home position sensor (S13) does not detect that the exit roller is at the upper position after the stack exit roller shift motor (M6) has been driven in the specified time when the exit roller is moved up.
Code: CC20
Description: Saddle communication error [MJ-1108]
Causes: Interface PC board (I/F) Finisher control PC board (FIN) Saddle control PC board (SDL)
Remedy: MJ-1108 Interface PC board (I/F) • Connector check • Harness check Finisher control PC board (FIN) • Connector check • Harness check Saddle control PC board (SDL) • Connector check • Harness check Interface PC board (I/F) Board check Finisher control PC board (FIN) Board check Saddle control PC board (SDL) Board check Finisher control PC board (FIN) Update the firmware version of the finisher control PC board (FIN). Saddle control PC board (SDL) Update the firmware version of the saddle control PC board (SDL).
Code: CC30
Description: Stack transport motor abnormality: The stack transport motor is not rotating or the stack transport belt is not moving normally. [MJ-1107/1108]
Causes: MJ-1107 Stack transport motor (M5) Finisher controller PC board MJ-1108 Stack transport motor Finisher control PC board
Remedy: MJ-1107 Stack transport belt If there is mechanical problem when the stack transport belt is moved, fix the mechanism. Stack transport motor (M5) Check the connectors and harnesses between the stack transport motor (M5) and the finisher control PC board (CN10). MJ-1108 Stack transport belt Move the stack transport belt. Fix any mechanical problem. Stack transport motor Check if the connector (CN17) on the finisher controller PC board is disconnected from the stack transport motor (M8) and the harnesses are open circuited. Correct if so.
Code: CC31
Description: Transport motor abnormality: The transport motor is not rotating or the stack transport roller -1 and -2 is not rotating normally. [MJ-1107/1108]
Causes: MJ-1107 Transport motor (M2) Finisher controller PC board MJ-1108 Transport motor Finisher control PC board
Remedy: MJ-1107 Stack transport roller If there is mechanical problem when the stack transport roller -1 and -2 are rotated, fix the mechanism. Transport motor (M2) Check the connectors and harnesses between the transport motor (M2) and the finisher control PC board (CN5). MJ-1108 Stack transport roller -1 Stack transport roller -2 Rotate the stack transport roller -1 and -2. Fix any mechanical problem. Transport motor Check if the connector (CN10) on the finisher controller PC board is disconnected from the transport motor (M7) and the harnesses are open circuited. Correct if so.
Code: CC41
Description: Paper holder cam home position abnormality: The paper holder cam is not at the home position. [MJ-1107/1108]
Causes: MJ-1107 Paper holder home position sensor (S6) Finisher controller PC board MJ-1108 Paper holder home position sensor Finisher control PC board
Remedy: MJ-1107 Paper holder cam If there is mechanical problem when the paper holder cam is rotated, fix the mechanism. Paper holder home position sensor (S6) Check the connectors and harnesses between the paper holder home position sensor (S6) and the finisher control PC board (CN17). MJ-1108 Paper pusher cam Rotate the paper pusher cam. Fix any mechanical problem. Paper holder home position sensor Check if the connector (CN9) on the finisher controller PC board is disconnected from the paper holder home position sensor (S6) and the harnesses are open circuited. Correct if so.