Các lỗi thường gặp

Code :
  • Code: 0002
  • Description: Sub CPU Communication Error
    Disorder of communication with Sub CPU
  • Causes: Sub Board does not work correctly. Sub CPU does not work correctly. There is a bad connection between Main Board and Sub Board.
  • Code: 0101
  • Description: Limit Position Erro
    rLimit Initialization in the Service Mode has not been done.
  • Causes: Limit Initialization in Service Mode has not been done.
  • Code: 0102
  • Description: Limit Sensor Error
    Even though the machine carries out the regular movement, the output of the Limit Sensor does not reach the expected value.
  • Causes: Limit Sensor does not work correctly or is broken.
  • Code: 0104
  • Description: Cap Unit Protection Error
    Even though the machine carries out the regular movement, the output of Cap Sensor does not become to reach the expected value.
  • Causes: Disorder of Cap Motor Fault of Cap Unit Fault of Cap Sensor Cut-line or short-circuit of Cable and Flexible Cable
  • Code: 0107
  • Description: Unset up of the Linear Encoder
    Linear Encoder Setup has not been done.
  • Causes: Linear Encoder Setup has not been done.
  • Code: 0108
  • Description: Wiper Unit Protection Errorder
    Even though the machine carries out the regular movement, the output of the Wiper Height Sensor does not reach the expected value.
  • Causes: Disorder of Wiper Height Sensor Fault of Wiper Unit Fault of Wiper Height Sensor Cut-line or short-circuit of Cable and Flexible Cable
  • Code: 0109
  • Description: Wiper Protection Error
    Even though the machine carries out the regular movement, the output of the Wiper Origin Sensor does not reach the expected value.
  • Causes: Disorder of Wiper Origin Sensor Fault of Wiper Unit Fault of Wiper Origin Sensor Cut-line or short-circuit of Cable and Flexible Cable
  • Code: 0110
  • Description: Linear Encoder Error
    Input value from Linear Encoder is not changed when Linear Encoder is set up the Origin. When Motor stops during printing, Motor does not complete the movement which is supposed to be done.
  • Causes: Read error of Linear Encoder Read error of Encoder on Scan Motor side Wire is not fixed to Head Carriage firmly.
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