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Code :
  • Code: F1-19
  • Description: Finisher/alignment motor trouble
    When operating the alignment motor, it does not move from the home position in 2sec. When operating the alignment motor, it does not return to the home position in 2sec.
  • Causes: Motor lock Motor RPM abnormality Overcurrent to the motor Finisher control PWB trouble
  • Remedy: Use SIM 3-3 to check the motor operation.
  • Code: F1-31
  • Description: Finisher saddle folding sensor trouble
    When the motor rotation speed (linear velocity) at every 200msec falls below the specified level. When moving to the home position, the home position sensor does not turn on within the specified time. When shifting from the home position to the lead edge, the home position sensor does not turn off within the specified time.
  • Causes: Sensor breakage Harness disconnection Console finisher control PWB trouble
  • Remedy: Use SIM 3-2 to check the sensor operation.
  • Code: F1-32
  • Description: Finisher-saddle communication trouble
    Communication error between the finisher and the saddle When the motor rotation speed (linear velocity) at every 200msec falls below the specified level. When moving to the home position, the home position sensor does not turn on within the specified time. When shifting from the home position to the lead edge, the home position sensor does not turn off within the specified time.
  • Causes: Improper connection or disconnection of the connector and the harness between the finisher and the saddle unit.
    Finisher control PWB trouble Control PWB (PCU) trouble
    Malfunction caused by noises
  • Remedy: Case 1 Cause Improper connection or disconnection of the connector and the harness between the finisher and the saddle unit. Check and remedy Check the connector and the harness in the communication line. Case 2 Cause Finisher control PWB trouble Control PWB (PCU) trouble Check and remedy Replace the finisher control PWB. Case 3 Cause Malfunction caused by noises Check and remedy Canceled by turning ON/ OFF the power.
  • Code: F1-33
  • Description: Finisher/punch shift motor trouble
    When operating the punch shift motor, it does not move from the home position in 4sec. When operating the punch shift motor, it does not return to the home position in 4sec.
  • Causes: Motor lock Motor RPM abnormality Overcurrent to the motor Finisher control PWB trouble
  • Remedy: Use SIM 3-3 to check the motor operation.
  • Code: F1-34
  • Description: Finisher/punch motor trouble
    When learning the punch unit, it does not complete normally and does not return to the home position. When executing punching, it does not shift from the home position in 0.2sec, or it overruns to go into non-HP state. When operating the punch unit, the encoder input cannot be detected within 0.1sec.
  • Causes: Motor lock Motor RPM abnormality Overcurrent to the motor Finisher control PWB trouble
  • Remedy: Use SIM 3-3 to check the motor operation.
  • Code: F1-37
  • Description: Finisher/ backup RAM trouble
    When backup RAM data check sum is NG when turning on the power.
  • Causes: Finisher control PWB trouble Malfunction caused by noises
  • Remedy: Replace the finisher control PWB.
  • Code: F1-38
  • Description: Finisher/punch backup ROM trouble
    Punch unit backup RAM data are garbled.
  • Causes: Punch control PWB trouble Malfunction caused by noises
  • Remedy: Replace the punch control PWB.
  • Code: F1-41
  • Description: Finisher/saddle positioning plate motor trouble
    The positioning motor HP sensor does not turn on within 1.33sec after starting the motor. The positioning motor HP sensor does not turn off within 1sec after starting the motor.
  • Causes: Finisher control PWB trouble Malfunction caused by noises
  • Remedy: Replace the finisher control PWB.
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