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Code :
  • Code: EAFA
  • Description: Finisher jam Paper Jam in Finisher - Please Clear Paper Path.
  • Causes: Catching motor home position detection error (paper jam)
  • Remedy:
  • Code: EAFB
  • Description: Finisher jam Paper Jam in Finisher - Please Clear Paper Path. Stapler movement error (paper jam)
  • Causes: Staple unit sliding motor (M7) Staple unit sliding home position sensor (S3) The turning OFF of the staple unit sliding home position sensor (S3) is not detected when the staple unit is moved from a point where this sensor is turned ON to one point where this sensor is turned OFF after the staple unit sliding motor (M7) has been driven at the specified number of pulse. The turning ON of the staple unit sliding home position sensor (S3) is not detected when the staple unit is moved from a point where this sensor is turned OFF to one point where this sensor is turned ON after the staple unit sliding motor (M7) has been driven at the specified number of pulse
  • Remedy: Staple unit sliding motor (M7) abnormality Check if the electrical continuity of the coil is normal. If electricity is not conducted, replace the staple unit. Staple unit sliding home position sensor (S3) abnormality Measure the voltage on TP18 on the finisher control PC board (FIN). Then check that the measured voltage is 1V or lower when not shielded and within the range of 3.3V+-5% when shielded. If the voltage does not fall within the range mentioned, replace the sensor. Faulty cables and connectors Check if the electrical continuity between the connector terminals is normal. If electricity is not conducted, replace the connectors. (Finisher control PC board (FIN): CN3, CN18) Finisher control PC board (FIN) abnormality If the error still occurs after replacing the staple unit, sensors and connectors, exchange the finisher control PC board (FIN).
  • Code: EAFC
  • Description: Finisher jam Paper Jam in Finisher - Please Clear Paper Path. Movable tray height error (paper jam)
  • Causes: Movable tray shift motor (M12) Movable tray position A, B, and C sensors (S13, S14 and S15) Finisher control PC board (FIN)
  • Remedy: Movable tray If there is mechanical problem when the movable tray is moved, fix the mechanism. Movable tray shift motor (M12) Check the connectors and harnesses between the movable tray shift motor (M12) and the finisher control PC board (CN19). Movable tray position A, B, and C sensors (S13, S14 and S15) • Connector check (CN20) • Sensor check • Harness check
  • Code: EAFD
  • Description: Finisher jam Paper Jam in Finisher - Please Clear Paper Path. Movable tray movement error (paper jam)
  • Causes: Movable tray paper-full sensor (S16) Movable tray position A, B, and C sensors (S13, S14 and S15) Finisher control PC board (FIN)
  • Remedy: Movable tray paper-full sensor (S16) Fix any mechanical problem occurring when the actuator is moved. Check if there is a disconnection of the connector, incorrect installation or breakage of the movable tray paper-full sensor (S16). If there is, reinstall the sensor correctly or replace it. Check if the connector (CN22) on the finisher controller PC board is disconnected from the movable tray paper-full sensor (S16) and the harnesses are open circuited. Correct if so. Movable tray position A, B, and C sensors (S13, S14 and S15) • Connector check (CN20) • Sensor check • Harness check
  • Code: EAFE
  • Description: Finisher jam Paper Jam in Finisher - Please Clear Paper Path. Paper holder cam position error (paper jam)
  • Causes: Assist arm motor (M10) Finisher control PC board (FIN)
  • Remedy: Paper pusher cam • Is there any mechanical problem when the paper pusher cam is rotated? Assist arm motor (M10) • Motor check • Connector check (CN10) • Harness check Finisher control PC board (FIN) • Connector check (CN10) • Board check
  • Code: EAFE
  • Description: Paper holding cam position error (paper jam)
  • Causes: Assist arm motor (M10) Finisher control PC board (FIN)
  • Remedy: Paper pusher cam • Is there any mechanical problem when the paper pusher cam is rotated? Assist arm motor (M10) • Motor check • Connector check (CN10) • Harness check Finisher control PC board (FIN) • Connector check (CN10) • Board check
  • Code: EB30
  • Description: Other paper jams Paper Jam in Printer - Please Clear Paper Path. Ready time-out jam
  • Causes: LGC board
  • Remedy: Finisher Check if the connector on the equipment is disconnected from the finisher or the harnesses are open circuited. Correct if any.
  • Code: EB50
  • Description: Paper transport jam Paper Jam in Printer - Please Clear Paper Path. Paper remaining jam on the transport path
  • Causes: Feed sensor CFD board LGC board Separation roller, Separation pad
  • Remedy: Feed sensor • Sensor check (Perform the input check: FS-03-[ALL]OFF/[9]/[B]) • Connector check (J790, CN404) • Harness check CFD board • Board check • Connector check (CN404, CN408) • Harness check LGC board • Board check • Connector check (CN369) • Harness check
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