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Code :
  • Code: 041-210, 041-211
  • Description: STM NVM Out-Of-Order/ STM NVM R/W Error [STM NVM Out-Of-Order] The NVM of the STM is malfunctioning. [STM NVM R/W Error] Unable to perform NVM Read / Write for the STM.
  • Remedy: 1. Turn the power OFF and ON. 2. If the problem persists, replace the STM PWB. (PL 10.6)
  • Code: 042-325, 042-614
  • Description: Main Motor Rotation Error/ Main Motor Rotation Warning [Main Motor Rotation Error] The Main Drive Motor revolution failure was detected. When the Lock Up (Main Drive Motor Fail) signal of the Motor Drive output was monitored at the specified time interval after a certain time has passed since the Main Drive Motor operation had started, it was found to have failed 5 times in a row. [Main Motor Rotation Warning] The Main Drive Motor revolution failure was detected. When the Lock Up (Main Drive Motor Fail) signal of the Motor Drive output was monitored at the specified time interval after a certain time has passed since the Main Drive Motor operation had started, it was found to have failed 2 times in a row.
  • Remedy: Enter the CE Mode and turn ON the Output Check [042-001] (Main Drive Motor). Does the Main Drive Motor rotate? Y↓N→Check the power supply line (+24VDC, +5VDC) of the Main Drive Motor. Is the power supply of the Main Drive Motor normal? Y↓N→Check the power supply circuit to the Main Drive Motor. Turn OFF the power and check the following: • The connection between the Main Drive Motor J202 and the ESS/MCU PWB J403 for open circuit, short circuit, and poor contact. • The Drive Gear for wear, damage, and bearing blockage. • The Main Drive Motor for loading. If no problem is found, replace the following parts in sequence: • Main Drive Motor (PL 3.1) • ESS/MCU PWB (PL 18.3) Press [Stop] and turn OFF the power. Check the connection between the Main Drive Motor J202-8 and the ESS/MCU PWB J403-5 for open circuit, short circuit, and poor contact. If no problem is found, replace the following parts in sequence: • ESS/MCU PWB (PL 18.3) • Main Drive Motor (PL 3.1)
  • Code: 042-400
  • Description: Smell Life Over BSD-ON: The Odor Filter is due for replacement.
  • Remedy: • Replace the Odor Filter and clear the VOC Filter HFSI Counter (950-805: FCOUNT_SMELL_HFSI_COUNTER).
  • Code: 042-608
  • Description: Voc Life Over BSD-ON: The Voc Filter is due for replacement
  • Remedy: • Replace the Voc Filter and clear the VOC Filter HFSI Counter (950-806: COUNT_VOC_HFSI_COUNTER).
  • Code: 045-310
  • Description: Image Ready Error Unable to send the Image-valid signal cannot within the specified time. NOTE: When the attempt to expand the image has failed, [016-776 Marker Code Detection Fail] occurs after the recover operation.
  • Remedy: 1. Check the following: • The Net Cable for poor connection. • The USB Cable (Local) for poor connection. • The connector ( P/J425) between the ESS/MCU PWB and the NET I/F PWB for poor contact. 2. Upgrade the Controller Firmware. ADJ 18.2.3 3. If no problem is found, replace the ESS/MCU PWB. (PL 18.3)
  • Code: 045-313
  • Description: IOT Logic Fail The IOT Software error was detected
  • Remedy: 1. Turn the power OFF and ON. 2. Install the correct version of the IOT firmware. 3. If the problem persists, replace the ESS/MCU PWB. (PL 18.3)
  • Code: 047-218
  • Description: MCU-2TM Communication Error Communication failure between ESS/MCU PWB and 2TM PWB was detected.
  • Remedy: 1. Check the connections of the following connectors: • ESS/MCU PWB J413 • STM PWB J541C/ J413C • 2TM PWB J541 2. Check the following harnesses for open circuits and poor contacts: • Between ESS/MCU PWB and STM PWB • Between STM PWB and 2TM PWB 3. If no problem is found at 1 and 2, replace the following parts in sequence: • 2TM PWB (PL 11.6) • STM PWB (PL 10.6) • ESS/MCU PWB (PL 18.3)
  • Code: 061-321
  • Description: ROS Motor Fail The number of rotation of the ROS Motor did not come within the standard range within the specified time (5 s) after the ROS Motor On.
  • Remedy: 1. Turn the power OFF and ON. 2. Check whether the Drum Cartridge is installed. 3. Check the ROS Motor (Output Check [061-001]) for operation failure. 4. Check the LD +5VDC power supply of the LD PWB J140 pin-8. 5. If no problem is found, replace the following parts in sequence: • ROS Assembly (PL 2.1) • ESS/MCU PWB (PL 18.3)
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